V1945G103NF3

Assistant EO, weeks 1, 2, 3


B-29 mechanics 102

Packaging Horsepower

Engine combat life = 97 hours

“Blow By” Crew

Write URs to Wright Field on Failed Engines

Valve Failure Pattern Puzzle

Changing Cylinders a Bloody Job

Bernard B Bugg

Bomb sight mod for Jet Stream

Electrical Solution

Clipping Trees on Take Off

Hardstands the B-29's Home

Pre Take Off

Prop Clips Parks Cap

Engine Noise and Liquid Locks

Stand by Crew

Lift off, two per minute

Weaving through Traffic

Bomb Shackle problem

Incentive

Fuel Tank Flak Damage

Solenoid failures

Electrical to Pneumatic Doors

Keough to Group EO

Landau to Sqd EO

Reason for Valve failure pattern

Valve Failure Fix – too Late


            B-29 Mechanics 102    Following my first days lesson I continued, going from plane to plane working as a crew member, becoming acquainted with them and learning more.  During my flight line time on Guam I learned something new almost every day.  Those of later generation are unaware of how rapidly technology was changing, every aspect of weaponry and infrastructure.  The farming region where I grew up was being powered by horses, mules and manual labor when I began learning about things.  Our first family car was a 1928 Model-A Ford, my fathers “company car” was a 1923 Model-T Ford.  My first car in high school was a 1927 Model-T that cost $5.00 plus $4.00 for a car tag.  That car was my B-29 maintenance trainer, later upgraded to a  $40 1932 Model-A maintenance trainer.  I did well in my first class in airplane mechanic because I’d learned how to use hand tools from a Black Smith, threading U bolts when I was in grade school. 

            There was a huge demand for skilled mechanics and all of the better ones had learned much, as I did, before going into service.  Military aptitude tests had assured a supply of capable people into the ground crew ranks, I found that crew chiefs and specialist ground crew were well above average intelligence – you can’t judge a man’s capability by their appearance, one of the brightest guys on the flight line looked dumb as a clod.  I was proud to be learning from some of the best.

            The B-17 was flying with a 1932 designed engine, the B-29 was flying with a 1942 designed system rushed into service before the bugs had been worked out.  The first day I realized B-29 engines were the primary maintenance problem.  Many of the flight crew were unaware of the maintenance required because they always took off with good engines, unaware an engine had been replace while they slept.  A “power plant” is a system and not just and engine. From day one I focused on how this power plant was packaged.

Packaging Horsepower

18 pistons with 3350 cu in displacement must breath hard to produce 2200 hp. Granddad never dream that many horses could be harnessed to one pull point – let alone hitch four wide to fly higher than Santa’s Reindeer.   Real horses use sweat for liquid cooling.  “No Sweat” did not apply to cooling B-29 horse power.  They were air cooled and un-intended turbulence caused some to became burnt toast, oil cooked to carbon, but you can’t see turbulence or cooked oil, cockpit temperature readings were not reading the hottest.

Breathing air entered at chin level before being turbo-compressed and piston-sucked (push-pulled) through a filter to carburetor mixing air with metered gasoline – then ignited.  Carburetors are mechanical computers for metering fuel to match air flow.  Exhaust was collected front and back to power left and right superchargers.

Cooling air flowed past the propeller hub and inside minimum drag cowling – through an annulus gap in a torturous path to an exit metered by cowl flaps set by the flight engineer.  Engines were suspended on shock mounts and moved inside the fixed outer cowling, forward exhaust stacks had flex joints at the engine to allow for engine movement. Cowling skin was removable for access to align these droopy tubes and replace spark plugs.  The system was a masterpiece of air flow management – a special blend of geometry and thermodynamics. The engine kinematics were the result of an evolutionary process.  There was one crankshaft with a master front and aft connecting rod, to which 8 articulating rods attached. 

Intake and exhaust valves are opened by rocker arms (a pivoted titer-totter) at the top.  Valve springs close the valves and push rods, lifted by a cam plate in sync with the crank shaft, pushed the rocker arm, overcome the spring force and hold valves open for a proper time. Valve timing is fixed and not adjustable.  There is valve opening overlap where inlet helps clean out exhaust.

Each engine was fitted with a 60 gallon supply of oil, pumped to and from the engine.  Valve lubricating oil went up inside push rods to lubricate brass valve guides and returned inside push rod covers.   Changing individual cylinders was possible, but difficult.  Since the failure of one cylinder was a precursor to pending other failures it was pragmatic to change the entire engine.

            An engine change could be achieved by one person, however it required many hands to hold the nine flex joint exhaust extensions when slipping the cowling on.

A time consuming tedious job was clamping the air inlet to the engine carburetor after engine installation.  This was done with a quite long bolt with fine threads – fitting the bolt in place was the easy job – but tightening the nut could only be done with and open end wrench that had to be flipped after each movement to fit on the nut – while your body was inside the engine access port above the back of the engine, facing up.  Having done this many times I would sometimes relieve a mechanic so he could rest his contorted body and reset his disposition. 

There were more change modifications to the engines than to the airplane.  The aircraft and engine was designed after the war began and went into combat while still fixing flaws.  That’s me above, with left hand on the engine, which shows relative size.

Combat life of R3350 engines = 97 hours

In the urgency to deploy, a fixable flaw fell through the crack

I went to 314 wing hdq to obtain maintenance data on the R3350 engines, tech orders rated it’s life as 450 hours, I was shocked to find the average combat life was 97 hours.  Since an average mission lasted 12 hours, the average engine was good for 8 missions.  The ground crew had to replace one of the four B-29 engines every other mission.  While training in the states, B-29 engines did well to last 12 hours.  To win the war in the Pacific it was essential to make B-29’s available as fast as launch sites became available.  Gen Hap Arnold pressed to obtain new aircraft, new bases and train crews as fast as possible, none existed when the war began..  The program pressed on using flawed engines while incorporating improvement modifications.   It was known that exhaust valves failed due to over heating.  Modifications helped  but were not fixes – the program pressed on.

“Blow By” Crew

There was no simple way to know when an engine needed changing.  As a preventive maintenance effort Capt Keough established a “blow by” crew, R. Bixby and W. Driscoll.   Two mechanics, one on each side, on ladders place their ear to each exhaust and listened for faulty exhaust valve seating.  If an exhaust valve did not seat properly on the compression stroke, “blow by” could be heard.  Engines that failed this test were replaced before they failed in flight.  Due to this preventive maintenance 28th Sqd had the best maintenance record in the 314th wing, possibly the 20th AF.

Write Unsatisfactory Reports to Wright Field on Failed Engines

Burned off Exhaust Valve

After about a week and a half Keough said enough of your working as a mechanic, you know enough already.  I can’t keep up with things that need to be done, come with me.  He took me to a collection of some 20 removed engines, saying I want you to write UR (Unsatisfactory Reports that are sent to Wright Field) on these engines.  He didn’t elaborate on what or how.  I knew from things he’d told me that he’d given these failures much thought. I was sure Wright Field already had stacks of UR’s stating that burned off valves were the cause of engine failure.  I wanted to know why the valves failed, and knew Keough expected more than a simple answer.  I also had motive, I’d been up all night with mechanics trying to get engines changed in time for the pending mission.

            Flight crews filled out a Form 41A  stating known problems when they landed.  Ground crews maintained a Form 41B stating the status of a repaired airplane.  Most of the time engines with burn off valves would continue running and were reported as “engine running rough” or “oil leak on #3” – valve failures could also result in severe problems.

Removed B-29 engines on Iwo Jima

I decided to use a “speed wrench’ and remove all exhaust valve rocker covers and look at the status of all the valve stems – my gosh – in short order the cause became evident.  On certain cylinders lubricating oil to the exhaust valve stems had been cooked to carbon!  Why valves failed was obvious.  This had to be known to every engine rebuild center – exhaust valves got too hot.  I learned that Wright Field had come up with a fix, they were changing all new engines to use “fuel injection”, a carburetor is not used, gasoline’s is squirted into the cylinder so that “heat of vaporization” can cool the combustion chamber.  Wright Field assumed that all the cylinders were over heating.  However from the sample I had,  many of the cylinders were just fine?  Those in the upper right, as viewed from in back, were the only ones cooking oil to carbon.  All others were just fine?  The Wright Field solution did nothing for the huge numbers of engines already in service – this looked like a fixable problem..

            Exhaust valves were larger than intake valves and filled with sodium, which became liquid when hot and “splashed heat” from the valve head to the valve stem.  The valve stem cycled up and down in a brass sleeve bushing, pressed into a cast aluminum cylinder head with cooling fins.  If cooling could not keep up, the brass bearing would wear and the valve head not seat properly.  With improper seating thermal runaway began – cooking the lubricating oil and sometimes burning through the valve stem, leaving the valve head inside the cylinder.  The above photo shows such a hammered valve head.

            So why did some valves remain adequately cool and some not?  The engines were symmetrical with regard to cooling fins and air flow, except for a Propeller governor at the top and two ignition distributors on each side.  Those disrupted air flow, and is why the one and only temperature reading was on the top front master cylinder.  The flight engineer could read the status of the believed to be “hottest cylinder” with this thermocouple reading – and cut back power before the engine overheated.  However my sampling showed the top front cylinder was not the hottest – but why?  The prop governor in front of it should have caused it to be the hottest.

Boeing designed the engine cowling (aerodynamic engine cover) for minimum drag – however the B-29 was different than any other radial engine equipped airplane, it collected exhaust to power a turbo super charger.  Covering the forward exhaust collector ring, pinched off cooling air flow.  All believed there was adequate cooling so long as the flight engineer kept the temperature reading within limits.  In fact during high altitude cruise it was necessary to close the cowl flaps a bit to keep the engine warm.  Take off temperatures at low speeds were “hot”, be it KS or Guam, while high altitude air is very cold.

Why were Failures Skewed to Right?

I was stumped – why did most cylinders immediately behind the air flow obstructions stay sufficiently cool while others did not?   I completed my assigned task and made my findings known via my UR reports.  Keough found my findings and conclusions quite interesting.  Those prior to me were too hard pressed with immediate tasks, they didn’t have the time or the sample to study the problem – the condition was there for anyone to read.  I stopped work on this and put the puzzle on my back burner.

Cylinder Change, a Bloody Job

            Most of the Crew Chiefs had at some time changed individual cylinders in lieu of doing a complete engine change. What seemed a simple solution turned out to be a bear and the practice was avoided.  I learned of the difficulties first hand when one of the mechanics came to me with bloody hands and asked if I'd help him finish. The problem was access to the safety wire through the cylinder hold down bolts.

            The cylinder heads were of cast aluminum but the cylinder walls were steel with fused on sheet metal fins. These fins were stamped out of sheet stock and their edges were razor sharp. Without special tools one had to shove hands into the confined areas between the cylinders and work the stiff wire through the bolts with fingertips. There was no way to get this done on an installed engine without scraping or slicing knuckles or palms of ones hands. They'd bleed and be sore when you most needed them to work tools. We settled for some real crappy looking safety wire jobs but they were all safety wired.  At the time we didn't tumble to the fact that it was always cylinders in the HOT quadrant region that needed changing.

            Changing the #1 master cylinder was rare and required special care. As the cylinder was lifted off the piston, it was necessary to rig a holder to keep the master rod centered in the open port. All articulating rods, those to the other cylinders, connected to it. If it tilted beyond certain bounds, attached articulating rods would pull pistons too far into the crank case and the piston rings pop to full expansion making it impossible to put them back. The entire engine would need to be removed to correct the problem. Remove and Replace was not as simple as it might sound.

Bernard B Bug, Adjutant and Confidant

            Bernie, a most unusual character, lived in the opposite end of our barracks. He'd been trained as a navigator but became air sick, was grounded and assigned as Sqd Adjutant. He was quick, bright and liked by everyone and became the confidant to most crew members. His serious poker face veiled his active but dry sense of humor. The crews trusted him implicitly and he carried all sorts of instructions in his head or in special notes to be sure letters from girl friends were not sent to families, etc.

            My first contact was when Bernie asked me to loan him some money - he told me he needed $300 for a stake in a poker game. He didn't want to borrow from flight crews or those who gambled. I loaned him the money and he gave me $350 the next day. His poker face put him in good stead, no one knew of him being a loser after a nights play. He was often broke and borrowed money. Bernie sent his winnings home making sure he couldn't loose what he'd won!  His habit was to borrow to get into a game, some might have thought he’d been loosing.  Poker was played at the officers club with the standard ante being $25. This was usually in the form of bill's tied together. It was not a game for amateurs.

Jets Stream blows B-29's out to sea, Smitty modifies Bomb sight

            Near by bunk mates Smitty a ground maintenance Radar Officer, Brownell a ground maintenance Radio Officer and Pultz a de-briefing Intelligence Officer told me about early missions which were flown at high altitudes to evade flak and fighters. They encountered high velocity winds of over 200 mph. These were later called Jet Streams and used to advantage in commercial flying. It was found that when trying to fly into them to reach a target they were sometimes actually being blown away from Japan with a negative ground speed. Brownell told how Smitty had devised a new scale so they could correct for these strong winds which were beyond the Bombardiers Nordon bomb sight scale. They used Smitty's modified scale as an alternative until LeMay ordered a shift to low level bombing.

Electrical Problem Fix

            Electrical Specialists told me of unique solutions for early special problems.  The B-29 used many electrical systems and was a maze of wires.  Electricians found wires chewed on by rats, when baited traps didn't work they called Operations.  Operations send a crew equipped with old style oxygen masks to take the plane to high altitude and suffocate the rodents – it worked.

Clipping Off the Tree Tops

            Before I arrived M-6 was flown by Hans Gammel through Pati Point trees on take off,  Johnson was the crew chief.  About 1995 I met with Gammel and Vern Chandler and listened to Hans tell Vern of keep it in the air, passed the cliff and salvo their bomb load. Engine #4 was delivering power but vibrating due to it's damaged prop. They feathered the prop and began dumping gas as they swung about and landed mid island at Harmon Field.  Harmon Field was used for planes that had to return so as not to interrupt takeoffs from North Field. The Service Center and Johnsons crew soon had the plane repaired and on flying status again.  (Vern Chandler and Hans Gammel were 28th Sqd Airplane Commanders flying the same missions.  Vern found Hans was in a near by Texas hospital. Before going to see Hans, Vern made a model B-29, with limb poking from it’s right wing, and took it to Hans with best wishes.)

 

Gammel flies M6 through Pati Point tree tops during takeoff

 

Trimming trees with fully loaded B-29 is not recommended.

Hans Gammel M-6 crew

Hardstands the B-29's Home   Everyone worked from early morning at the steady efficient pace of men who knew their jobs and recognized they were working against the clock. In addition to basic repairs to the aircraft, the planes had to be turned around. The repair areas were black topped branches off the taxi strips called "hard stands". Some were short with room for one plane and some longer with room for two planes. Returning from the previous mission, the planes were taxied into the hard stands. They had to be towed out onto the taxi strips and backed into the hard stands so they could taxi out at take-off-time.

            The planes were normally turned around using a Cletrack before they were loaded with fuel and bombs. It was a real struggle to back a 70 ton loaded plane up even a slight incline.

            A hard stand could become very crowded. The maintenance crews required hoists and platforms in order to reach and work on the engines. It was essential for Ordnance people to have room for their bomb dolly's. Tank wagons and oil trucks needed access in order to load the 6700 gallons of gas in the wings and add 60 gallons of oil to each of the four engines oil tanks. The Armament people had to load the (10) 50 caliber machine guns.

Pre Take Off

M-10 ready to taxi out

            Few of the planes were ready when the flight crews arrived.  Ground crews were tired but working at a feverish pace to meet the deadline. The flight crews were sometimes tense before take-off-time and naturally finicky about the condition of the plane.  A squadron of 15 planes was bound to produce some sharp impatient exchanges.  In most cases there was much understanding an patience. The status of each plane had to be checked and ground crews shifted to help those having trouble meeting the deadline.

            Prop tip splits bill on Parks cap   Crew Chief Parks had an agreement with the Bombardier that Parks would hunching his back into the new air operated bomb bay door to latch it shut.   Crews would get in and out in and out and the air compressor could not keep pressure up.  This worked fine till a new Bombardier, seeing the door did not latched flipped it to open and try again.   Parks found he was being pushed down as the air compressor built pressure.  Engines were running and he could not be heard.  Aware his head was inline with the prop blade he decided he’d better drop to the ground fast before pushed into the prop blade.  When he dropped the blade flung his cap off.  When he recovered it he found the prop tip had split the tip of his ball cap.  With the compressor recharged the door latched and the plane taxied out.  You can be assured Parks didn’t let that happen again.

            Engine Noise   The whole area became an inferno of engines being given final checkout. Each of the 60 engines had to be run to full power. Torrents of air whipped the landscape. Conversation in the vicinity of a plane was impossible except by shouting in the person's ear, hand signals were used when practicable.  As the planes were turned over to the flight crews the inferno would diminish and permit identification of those having trouble. Troubles came in all kinds of packages. The obvious ones were of crews trying to clear fouled spark plugs by running up engines to 2/3 power for longer than normal periods or those bellowing black smoke and backfiring due to flooded engines. The carburetors rarely malfunctioned but an engine could be over primed at start up and bellow smoke till the carburetor took over.

            Radio and Radar people had to service their sets.  Armament had to check guns and service the automatic fire control systems.  Electrical and instrument specialist had to check automatic flight control systems, instrument panels, control mechanisms auxiliary power supplies, cabin pressurization systems, photo, navigational systems, etc., including the thunder mug. All these people competed for access in and around the plane.

            Liquid locks:   Invariably there was a liquid lock where oil had settled into the piston heads of the bottom cylinders. With the valves closed the engine would not rotate in the forward direction. The orthodox remedy was to remove a spark plug and drain the oil, but which one or ones? This method took time and delayed take off for that plane. An unorthodox remedy, described later, was technically all right and quite pragmatic, but got us in trouble.

Standby Crew at Take Off

            There were many types of problems that required hurried trouble shooting to find the fault and led to tedious frustration in accomplishing a repair in time. As take-off-time arrived the planes would move out into single file along the taxi strips.  When the flight crew took over the ground crew would gather at the engineering tent – they would not leave until they saw their plane lift off, then they would go to the 6x6 and fall asleep pending a full load for the trip to mess hall. 

A “Stand By Crew” took their place in the Weapons Carrier (a pickup type truck) and the Line Chiefs would join the Engineering Officer in the jeep.  As ground crew would gather around the Engineering tent the Crew Chief would report as his plane taxied out and join his crew to watch for their plane to come down the runway.

Standby crew in Weapons Carrier or Jeep would weave their way to plane in trouble.

            180 B-29's lined up for take off is a noisy, windy, dynamic sight but attention was focused on the runways. Engines had to be driven to maximum power to lift the 10 ton bomb load and a 16 hour fuel supply, they lifted a load equivalent to that of (5) B-17's, for a distance equivalent from Los Angeles to Chicago and back with a crew of 11. The armament and armor plating was a considerable load in itself without the bombs. The same engines were used by airlines after the war. However, they were asked to deliver 1/2 the horsepower.

            As each plane came down the runway it's ground crew listened to the pitch of its engines, watch the color of the exhaust and look for hot spots.  Turbo superchargers driven by exhaust gases from the engines pumped extra air into the engines for take off. Each ground crew member watched for any kind of fault symptom as their plane roared down the runway.  When their plane lifted off and dropped out of sight when past Pati Point cliff, they walked past Keough’s Jeep saying M-2 is off OK and climbed in the 6x6 truck for the ride back.  They were too tired to be interested in the dynamic spectacle - they'd seen it many times before.

             Two Lift off per minute:  Planes took off at one minute intervals on each of the two runways, a plane became airborne every 30 seconds. Even so a take off could span a two hour period in case of problems.

            Weaving through traffic  A plane in take off cued with a problem would call the tower, the tower called the engineering tent and word yelled to the Standby Crew of the planes number and location. Keough’s Jeep would take the lead in a “mad dash” past, through and around planes advancing toward take off position. The canvas Jeep top would be caught in the slip stream of an engine revved up to move a plane ahead to take up slack in the queue line. If caught from the side, the blast would almost blow the Jeep over. Typical of such problems was that the copilot would open his window while waiting in the taxi line up and then not be able to close it.  One of the "Specialists" would run to the plane climb in and in a few moments return with the window shut. The plane would retain its taxi position.   We were always thankful a fixable thing was the extent of the problem.  It was a good take off if there were no aborts; ie, planes that started but didn't deliver.

  

A shackles was a manual or electrical commanded device for connecting bombs to Bombay support structure. 

Bomb Shackle Problem

The morning after completing the UR report on engines Keough said, come with me.  I followed Keough to look at bomb shackles scattered about a hard stand.  Keough said Ordnance should pick these up and not leave them where equipment can run over them and people slip on them.   Bomb shackles mount on bomb racks and clip on bombs to hold them in place.  They are equipped with a manual and electric release, so the bombardier can release one or many. 

            Ordnance personnel, tired after hours of sweaty work loading bombs, would leave extra shackles not needed for a particular mission on the hardstand. Though rugged these mechanisms were vulnerable to being run over by Cletracks, fuel trucks, etc.  They were disliked by the maintenance crews who'd sometime slip on them and fall, another frustration they didn't need. Keough felt these were sufficiently complex mechanisms that they should be stored so as not to be smashed and unreliable. Ordnance claimed they didn't use them if damaged, besides they didn't work for Keough.

Varied Bomb Loads

Number

Bomb Weight

Total Weight

80

100

8000

56

300

16800

40

500

20000

12

1000

12000

12

1600

19200

8

2000

16000

4

4000

16000

            The tables combinations of bombs are for bombs only with out bomb bay tanks. 

Bombay Fuel Tank

Take off weight was mission dependant.  One bomb bay fuel tank weight would be 4232 lb allowing 500 lb for the tank, 640 gal per tank and .70 specific gravity for gasoline. Consuming 1/4 bomb bay capacity it could be 85% of a max load.  500 lb incendiary clusters were bulky and full count would not fit, 18650 being a max load. 

  

   2/Lt D. Landau, 1/Lt R Heinze & Capt _____  Ordinance      Ordnance building and tents.

I piled some shackles in the jeep and took them to the Ordinance tent and encountered three officers; two 1/Lts and a Capt, I’d never seen before sitting in the tent door way.  I unloaded the shackles at their feet saying, “ Keough said he wanted these picked up.”  They said, “we don’t take orders from Keough.”   Pause – I said, “well I do take orders from Keough, and by the way I agree with him, they are in the way and subject to damage.”  As I started the Jeep to leave they called out,  “your as much of an SOB as Keough.”  I understood why Keough sent me -- he’d been doing battle with ordinance for some time. 

Ordinance needs an incentive   I recalled when M-6 was given a full power check it would almost blow the Ordinance tent away.  I went to crew chief Johnson and told him “our problem” and asked him to aim M-6 a bit more toward the Ordinance tent and give it a full power test – to almost but not quite blow their tent away.  Johnson smiled and did that.  When I arrived with the next batch of shackles I dumped them at their feet again, smiled and said, “gentlemen this has a simple solution: you pick up your shackles and we will take care to not blow your tent away.”  I sustained a grin while looking them in the eye.  I watched their scowls give way to grins as the better option.  In fact we became good friends, probably because of that.  I never spoke to Keough about this, but know Johnson told him why the shackles were being picked up.

Fuel Tank -- Flak Damage

            I helped replace a wing fuel tank damaged by flak, such maintenance was time consuming and difficult, we were not equipped to handle such things. Wing jacks had to be placed to lift-twist the wing so the phillips head screws could be removed to get the tank out.  The tanks were large, heavy and awkward to handle.  The reverse process of installing the tank was more difficult. It was difficult to align hole through skin and doublers to match screw hole in the structure.  Wing jacks were used to distort the wings in order to align plates and doublers with the screw holes. There were many, many closely spaced screws, designed for a very tight fit as they were under high stress as wings flexed in flight.  I was called upon to help by those whose arms and wrists had just given out. I soon understood their difficulty. We used drift pins to align and jacks under the screw driver to keep it engaged. The torque required was considerable placing excessive strain on the wrist. My wrist was sore for some two months after three hours helping fellows finish.   B-29 operations would have been greatly impaired if enemy flak had repeatedly punctured fuel tanks. Fortunately it was seldom.

Momentary Duty Fuel Valve in Leading edge

            Some Boeing engineer chose to use a momentary duty coil to latch a fuel transfer valve under the leading edge.  Some flight crew members didn't know it was designed for momentary use.  For inexplicable reasons they would hold the switch on and burn out the solenoid coil making it necessary to remove and replace the leading edge of the wing to get at it. We cussed the Boeing design and the crew member for sleeping on the switch.  The only access was to remove the leading edge between engine nacelles.

Electrical to Pneumatic Bomb bay Doors

Early model B-29's had electrically operated doors and newer planes had pneumatically operated doors. M-3 and M-11 used the old kind.  At start up a planes created a calliope of sounds, the air compressor for operating the bomb bay doors was a new one.  The electric doors were slow. An electric motor turned a long threaded shaft that had a high gear ratio to overcome the aerodynamic loads on the large doors.   Some planes had experienced sever structural loads, pulling G's to evade search lights or when caught in thermals from massive incendiary bomb raids.  One of the planes had been so badly bent that when loaded with bombs a motor was burned out just closing the doors. This was replaced before take off and another given to the Bombardier as a spare. I was present just before take off when Keough and the crew chief were showing the Bombardier how to change the motor in flight if necessary. It was to be used for closing the doors if the new motor just installed failed after opening the door.   This was a new crew and not happy about the procedure.  The Bombardier complained to Keough, "this damn thing is warped!" Keough responded, "You’d be warped too if you had as many missions." Sometimes Keough had a short fuse.  I’m sure Operations had told Keough to keep that plane flying rather than pull it for modification.

If a crew aborted a mission Operations would call Keough to find out if there had indeed been a problem, they knew they'd get a straight and honest answer.   One returned claiming an engine was emitting smoke, the ground crew could find nothing wrong.   A check revealed the "smoke" had been a vapor trail and the crew sent back in the air again – Operations was demanding.

Keough becomes 19th Bomb Group Engineering Officer

Landau becomes 28th Sqd Engineering Officer

            I had been there about three weeks when Keough was abruptly moved up to Group Engineering Officer, the Capt became Major.  Major Keough turned “his” 28th squadron over to 2/Lt Landau.  I was taken by surprise because in doing this several more experienced 1st Lt's were by bypassed, the table of organization called for a Captain and they would have advanced a grade.  I didn’t have enough time in grade so remained a 2nd Lt.  I pondered this.  I recalled him having private conversations with the crew chiefs before I was told, but I had a feeling solving his running battle with Ordnance had something to do with it.   Thankfully I received wonderful support from everyone.  Now many tasks handled by Keough became my responsibility, again I had to adapt and learn fast, which was only possible with the help of top notch Flight Line personnel.  They solved most of the problems; each day I learned more.

Keough was advanced because the prior 19th BG EO was sent to Okinawa to help set up operations there.  A later Keough told me I was to be the Engineering Officer of a new 4th Squadron to be added to the Group. I doubt if those doing the planning had any idea there was an Atomic Bomb.

Answer to the valve heating puzzle

The answer came when standing in front of a B-29 being run up for engine change ground test, prior to flight test.  I noticed how the propeller lifted water up, swirling it like mist through the front cooling air annulus – my gosh, that was it!  Cooling air did not flow back over the engine, it swirled at an angle, behind the propeller governor.  This was why the cylinders down stream at an angle from the Prop governor were the ones deprived of adequate cooling air. Why hadn’t I taken note of that before -- why hadn’t others? 

A solution  use Oil as Coolant

Each engine had a 60 gal oil tank with cooled engine oil, one pump fed oil to the engine and two “sump” pumps carried it back to the tank.  There was plenty of liquid coolant on hand.  We could use the front sump pump to pump cooling oil to the over heated valve region, the oil could flow back, as always, through the push rod housing.  We could carry cooling oil up from the front of the engine, behind push rods, and not cause extra drag, and feed it through holes in mounting studs to inside the rocker arm covers.  Modification kits could be made and installed at engine build up.  Thus cooled, these engines should last as long as R-2800 used on P-47’s and B-26’s ,with 2000 hours rated service.  I sketched a design on how to do this and gathered parts to modify an engine – then the war ended – after which nobody gave a damn about improving engine life.  Had the engines been so modified we could have flown missions every other day rather than every third day interval -- if bombs and fuel were supplied fast enough.  

How did problem fall through crack?

Engines were designed, manufactured and qualification tested in the time honored way, and passed qualification tests with flying colors.  Boeing fine tuned the engine installation after Eddie Allen, the Chief engineer and test pilot, was killed due to an engine failure and fire – a failed engine was not a Boeing problem.  Flight testing, normally done by Boeing, was taken over by the military and a senior pilot with combat experience put in charge.  Though the engine failures screamed for attention, the Col in charge officially wrote them off as “due to hot Kansas summers”

If qualified engineers had been assigned to fix the problem it could have been done in the early test phase.  The right people were not in the right place at the right time.  The US was in very short supply of trained engineers.  The one in charge would need to insist that the problem be fixed and not patched.  Without a failed sampling to draw from, as I had, a qualified engineer would needed to instrument tests to map temperatures – when running the engine inside an engine nacelle.  That would be easy ten years later using transistor technology. At the time it was very difficult.  It would be necessary to run thermocouple wire from each test point to special ammeter – which could be done on the ground.  This would have shown that the top cylinder was not the hottest.  A quick fix would be to put the thermocouple on the hottest cylinder, so the flight engineer got a true reading of engine status.  Once a thermal map was known there would be multiple options on how to how to cool the cylinders. 

The damage took place during take off, continued use did not clear damage done, damage accumulated.  Maj Chandler, typical of flight crews, was unaware of the magnitude of the engine change problem.  His rough running engines were always replaced before his next mission.  All knew engine problem were common, but often accepted such problems a part of flying combat.  Operations could always continue by replacing engines.  Blissfully flight crews didn’t know – particularly those taking off from Tinian and Saipan, who didn’t have a 600 foot cliff to drop from and let engines cool.  122 hp of heat was applied to each exhaust valve from the moment of applied full power at a standing start with nil cooling air flow, till lift off and cruising speed air flow two minute later.  There was no cooling problem cruising at altitude.  Hot KS summers had little to do with it.

The engines had lasted long enough to win the war and all thoughts shifted to going home.  These engines become scrap replace by new engines using secondary injection.